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LT1376CS8-5 参数 Datasheet PDF下载

LT1376CS8-5图片预览
型号: LT1376CS8-5
PDF下载: 下载PDF文件 查看货源
内容描述: 1.5A , 500kHz的降压型开关稳压器 [1.5A, 500kHz Step-Down Switching Regulators]
分类和应用: 稳压器开关式稳压器或控制器电源电路开关式控制器
文件页数/大小: 28 页 / 235 K
品牌: Linear [ Linear ]
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LT1375/ LT1376  
U
W
U U  
APPLICATIONS INFORMATION  
PARASITIC RESONANCE  
voltages over 1V lasting longer than 10ns should be  
avoided. Note that 100MHz oscilloscopes are barely fast  
enough to see the details of the falling edge overshoot in  
Figure 7.  
Resonance or “ringing” may sometimes be seen on the  
switch node (see Figure 7). Very high frequency ringing  
following switch rise time is caused by switch/diode/input  
capacitor lead inductance and diode capacitance. Schot-  
tky diodes have very high “Q” junction capacitance that  
can ring for many cycles when excited at high frequency.  
Iftotalleadlengthfortheinputcapacitor, diodeandswitch  
path is 1 inch, the inductance will be approximately 25nH.  
Schottky diode capacitance of 100pF will create a reso-  
nance at 100MHz. This ringing is not harmful to the  
LT1376 and can normally be ignored.  
A second, much lower frequency ringing is seen during  
switch off time if load current is low enough to allow the  
inductor current to fall to zero during part of the switch off  
time (see Figure 8). Switch and diode capacitance reso-  
nate with the inductor to form damped ringing at 1MHz to  
10 MHz. Again, this ringing is not harmful to the regulator  
and it has not been shown to contribute significantly to  
EMI. Any attempt to damp it with a resistive snubber will  
degrade efficiency.  
Overshoot or ringing following switch fall time is created  
by switch capacitance rather than diode capacitance. This  
ringing per se is not harmful, but the overshoot can cause  
problems if the amplitude becomes too high. The negative  
voltage can forward bias parasitic junctions on the IC chip  
and cause erratic switching. The LT1376 has special  
circuitry inside which mitigates this problem, but negative  
INPUT BYPASSING AND VOLTAGE RANGE  
Input Bypass Capacitor  
Step-down converters draw current from the input supply  
in pulses. The average height of these pulses is equal to  
load current, and the duty cycle is equal to VOUT/V . Rise  
IN  
and fall time of the current is very fast. A local bypass  
capacitor across the input supply is necessary to ensure  
proper operation of the regulator and minimize the ripple  
current fed back into the input supply. The capacitor also  
forces switching current to flow in a tight local loop,  
minimizing EMI.  
RISE AND FALL  
WAVEFORMS ARE  
SUPERIMPOSED  
(PULSE WIDTH IS  
NOT 120ns)  
5V/DIV  
Do not cheat on the ripple current rating of the Input  
bypass capacitor, but also dont get hung up on the value  
in microfarads. The input capacitor is intended to absorb  
all the switching current ripple, which can have an RMS  
value as high as one half of load current. Ripple current  
ratings on the capacitor must be observed to ensure  
reliable operation. The actual value of the capacitor in  
microfarads is not particularly important because at  
500kHz, any value above 5µF is essentially resistive. RMS  
ripple current rating is the critical parameter. Actual RMS  
current can be calculated from:  
20ns/DIV  
1375/76 F07  
Figure 7. Switch Node Resonance  
5V/DIV  
SWITCH NODE  
VOLTAGE  
2
IN  
INDUCTOR  
CURRENT  
100mA/DIV  
IRIPPLE RMS =IOUT  
V
V V  
/
V
(
)
OUT IN  
OUT  
(
)
20ns/DIV  
1375/76 F11  
The term inside the radical has a maximum value of 0.5  
when input voltage is twice output, and stays near 0.5 for  
a relatively wide range of input voltages. It is common  
0.5µs/DIV  
1375/76 F08  
Figure 8. Discontinuous Mode Ringing  
17